The activation of a new operating mode is not possible, the error code is sent as the response to the activation command. Homing to positive limit switch or negative limit switch is disabled. A parameter modification requires the drive to be powered off and on. Not possible to determine the commutation angle at the end of the wake and shake procedure. Welcome to the Schneider Electric corporate Website, Access mySchneider, your personalized digital experience. Improve EMC, verify grounding and shield connection. Command needs a valid zero point (ref_ok=1). Cyclic communication: The selected cycle time tolerance is too high. Connected type of EnDat encoder is not supported, Configuration error detected: Invalid SSI encoder parameter setting. Wait for the motion blend to complete before setting the next position. More than one signal positive limit switch/negative limit switch/reference switch active. Contact your Schneider Electric service representative. Safety function STO was activated while the power stage was disabled. PDF 9. Drive Fault Codes - Wireless Telemetry The Quick Stop option code has been set to -1 or -2 which causes the drive to transition to the operating state 9 Fault instead of the operating state 7 Quick Stop Active. The selected type of usage of the analog inputs is not possible. The acknowledgement signal is available for more than 6 seconds. Drive in operating state Quick Stop Active. Perform a Fault Reset. Set a speed limit not equal to zero for multiple SLS. Capture input 1 has not been set to both edges (IDN169). Reference switch error detected (switch signal briefly enabled or switch overtraveled). Incorrect setting for parameter WakeAndShakeGain. The positions scaling factor is set to a value less than 1rev/131072usr_p, which is less than the internal resolution. In this video we are going. The recalculation must be started after the initialization. Resolver: Signal communication subject to interference, System error detected: Encoder module RES is not ready for position evaluation. The selected operating mode is not available. In the operating modes Homing and Jog, the movement is internally interrupted by an internal software stop. Delay for reaching Safely Limited Speed (SLS) too low or eSM deceleration ramp too high. Command not permissible while the power stage is enabled (operating state Operation Enabled or Quick Stop Active). Access occupied by another channel (for example: Commissioning software is active and fieldbus access was tried at the same time). The position difference between the index pulse and the switching point is insufficient. Start Autotuning when the drive is in the operating state Ready To Switch On. Use a differently sized motor that can withstand the load torque. Privacy Policy. Resolver: Loss of signal, position unreliable. If the quasi absolute function is active, only power down the drive if the motor is at a standstill and do not move the motor shaft when the drive is off. File cannot be uploaded: Incorrect file ID, Data stored after a power outage is invalid, System error detected: No bootloader available, Configuration error detected (additional info=Modbus register address). Change POSscaleDenom and POSscaleNum in such a way as to increase the resulting scaling factor. System error detected: Incompatible data on the memory card, System error detected: Capacity of detected memory card insufficient, System error detected: Memory card not formatted, System error detected: Memory card is write-protected. Medium Voltage Distribution and Grid Automation, Product Documentation and Software Downloads, Panelboards / Switchboards and Switchgear, Controllers, Expansion Modules, Servers & HMIs, Power Metering and Energy Monitoring Systems, Power Quality and Power Factor Correction, Integrated Power and Control Solutions (IPaCS) Equipment, Low Voltage/Medium Voltage Prefab Substations, Pushbuttons, Switches, Pilot Lights, Control Stations and Joysticks, Data Center Security and Environmental Monitoring. Error detected by parameter management: Parameter (index) does not exist. System error detected: Timeout during connection to power stage, System error detected: Invalid data received from power stage, System error detected: Data exchange with power stage lost, System error detected: Exchange of identification data from power stage not successful, System error detected: Checksum identification data from power stage incorrect, System error detected: No identification frame received from power stage, System error detected: Type of power stage and manufacture data do not match, System error detected: Invalid numbers of data received, eSM module: System error detected: Error of class 1 forced, eSM module: System error detected: Error of class 2 forced, eSM module: System error detected: Error of class 3 forced, eSM module: System error detected: Error of class 4 forced, eSM module: Insufficient deceleration for Quick Stop. Set the operating state to Ready To Switch On and restart commutation offset identification. At least two analog inputs are configured with the same type of usage. No analog reference value source selected. This blog considers the cause of a motor overload fault (OLF) on Altivar drives. How to identify and resolve OLF faults on ATV drives problem with Schneider Altivar 71-error SCF1 | Electrician Talk Where can I find the list of fault codes for ATV61 drive? | Schneider The recalculation has been started prior to the initialization. Published for: Schneider Electric . Code W S1040 e 7005 Jog error detected (additional info = detailed error code). 2380 h. 9088. Command is being processed or communication may be disturbed (EMC). Manual tuning/Autotuning: Movement out of range. Use operating mode Homing to define a valid zero point. F007 Internal thermal sensor detected fault The drive temperature sensor is not operating correctly The drive is in short circuit or open Contact local Schneider Electric representative . E 1504 2 D5: Sine/cosine inputs exceed DOS out of range threshold. Holding brake cannot be released manually. Contact your Schneider Electric service representative. If you use the internal braking resistor, contact your Schneider Electric service representative. Verify the gear ratio in the operating mode Electronic Gear. Privacy Policy. The temperature parameters (in electronic nameplate of motor, non-volatile memory of encoder) are unavailable or invalid; parameter A12 is equal to 0. Return to the permissible movement range. System error detected: No memory card available, System error detected: Data on memory card and device do not match. Reference movements require limit switches. Motor overload fault (OLF) is triggered by the motor pulling current above the ItH (Motor Them Current) that is programmed into the drive. Configured debounce time not possible for this signal input function. The movement exceeded the adjusted movement range during Autotuning. Reduce velocity of the drive or verify eSM speed limit for machine operating mode Automatic Mode. Start your sales inquiry online and an expert will connect with you. Parameter changed that requires a restart of the drive. Easily find the nearest Schneider Electric distributor in your location. Find answers now. Limit switch or reference switch signal not defined for signal input function. Not possible to load parameters into safety module eSM. Library Diagnostic Codes Wait for Autotuning to finish before changing the parameter. You will receive your welcome message soon. Resolution of scaling too high (range exceeded), Change for jerk filter input position too great. Start operating mode Electronic Gear and/or select a gear method. Error detected during parameter check (for example, reference velocity value for operating mode Profile Position is greater than maximum permissible velocity of drive). Pulse duration must be less than 4 seconds. Reach out to our customer care team to receive more information, technical support, assistance with complaints and more. The motor requires a PWM frequency (16kHz) which the power stage does not support. Error detected by parameter management: Parameter (subindex) does not exist. NVE41289.03 www.schneider-electric.com Altivar Machine ATV320 NVE41289 01/2017 Altivar Machine ATV320 Variable Speed Drives for Asynchronous and Synchronous Motors Installation Manual Refer to manual or catalog. eSM module: System error detected: Boot program: Invalid address. Incorrect data length, insufficient number of bytes, Configuration download error detected (additional info=Modbus register address). System error detected: Invalid power stage data. Value in additional error information shows the Modbus register address of the parameter where the initialization error was detected. Please enter a valid email address, Problem with captcha verification, please check your connection. The values for the speed limits for multiple SLS are not in ascending order. eSM Disable requires the safety module eSM to be in operating state Operation Enabled. A start request for an operating mode has been received while a change of the operating mode was active. Position change in reference value for operating mode Electronic Gear too high. eSM module: Parameter checksum incorrect (default values loaded). Code 8503 / external diag. In this video we are going to see Schneider ALTIVAR ATV 310 VFD Drive fault code, Possible causes, and remedy part 1,(#schneider , #vfd )Welcome to controls. List of Fault Codes for ATV61 | Schneider Electric Support Watch on Published for: Schneider Electric USA Attachment (s) Command not permissible while power stage is active. The following information is available for each error message: The table below summarizes the error codes classified by range. Before triggering scaling, reset the parameters with user-defined units. - Change of handling of monitoring signals. Power the drive off and on again. The configuration of edges cannot be changed because difference value capture is active. Cyclic communication: Incorrect synchronization. The calculated offsets for the current sensors are out of range. Verify that the values of the mains power supply network comply with the technical data. If the detected error persists, deactivate the velocity observer. The Quick Stop option code has been set to -1 or -2 which causes the drive to transition to the operating state 9 Fault instead of the operating state 7 Quick Stop Active. Fieldbus module has been removed or fieldbus module is inoperative. Verify that the system can easily be moved. Excessive regeneration during deceleration. Develop more sustainable energy management and industrial automation applications powered by EcoStruxure. Different counting directions of motor encoder and machine encoder. 0:00 / 1:56 How to reset SLF Serial Link Fault on ATV312 | Schneider Electric Support Schneider Electric 175K subscribers Subscribe 167 58K views 7 years ago Step by step process for. Verify motor response after stopping and optimize control loop settings. Speed limit for multiple SLS in positive direction has a value of zero. From 6 long-term commitments to sustainability research and consulting, we are committed to being part of the solution by engaging our entire ecosystem in sustainable progress. Communication channel (Hiperface) to encoder is subject to interference or motor encoder is inoperative. The value entered was outside of the permissible value range for this parameter. Verify parameter configuration of ESMSTART. Connect an encoder to the input for encoder 1 before trying to set the absolute position directly via ENC1_abs_pos. Frequency of reference value signal is too high. Verify correct wiring of the inputs of the safety function STO and perform a Fault Reset. Privacy Policy. System error detected: Motor encoder inoperative, System error detected: Length specification for user data too great, System error detected: Communication with encoder not possible, Motor without electronic motor nameplate (for example, SER motor), No data segment of the electronic motor nameplate, System error detected: Motor configuration cannot be written, Not possible to write motor configuration, Incorrect encoder type selected with parameter MotEnctype, Error detected during the internal conversion of the motor configuration, Parameter of the motor configuration out of permissible range. Wait until the motor has come to a standstill (x_end = 1). If you only have the cheap little LED seven segment display screen this is tougher to navigate.
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